blondejoncherokee
NAXJA Member
- Location
- sacramento
XJ Updates:
good news! my ball joints are totally shot! I am so happy right now! all of them are totally fubar. That explains the wandering! I am going to grab new ball joints tomorrow and should be good to go!
I was in denial and refused to even check them since they are synergy and they are pretty new , maybe a year old? But both lowers are toast, like bad, and at least one upper, so that explains most of it. the front and rear bearings seem incredibly good .
WJ updates:
removed the drop pitman arm
cut off a welded on drop trackbar mount
drilled out stock mount for 5/8" bolt and the 3/4" heims
put a stock pitman arm back on
drives so much better.
DW seems to be gone
the major issue here was the drop trackbar mount dropped like 2" further than the drop pitman, wicked bump steer and probably causing some of the DW as well
I also have all the goodies to upgrade to the akebono calipers/rotors/pads and brand new timken unit bearings to go on, as well as all new TREs. Also have 4 brand new 5100s coming in the mail too. And some v249 tcase fluid coming too.
I also changed both diffs with royal purple 75-140 synthetic and changed both tranny filters and did 2.5 qts royal purple and 4 quarts ATF+4. I also added a drain plug to the tranny pan.
this thing drives so well, and more parts to come.
good news! my ball joints are totally shot! I am so happy right now! all of them are totally fubar. That explains the wandering! I am going to grab new ball joints tomorrow and should be good to go!
I was in denial and refused to even check them since they are synergy and they are pretty new , maybe a year old? But both lowers are toast, like bad, and at least one upper, so that explains most of it. the front and rear bearings seem incredibly good .
WJ updates:
removed the drop pitman arm
cut off a welded on drop trackbar mount
drilled out stock mount for 5/8" bolt and the 3/4" heims
put a stock pitman arm back on
drives so much better.
DW seems to be gone
the major issue here was the drop trackbar mount dropped like 2" further than the drop pitman, wicked bump steer and probably causing some of the DW as well
I also have all the goodies to upgrade to the akebono calipers/rotors/pads and brand new timken unit bearings to go on, as well as all new TREs. Also have 4 brand new 5100s coming in the mail too. And some v249 tcase fluid coming too.
I also changed both diffs with royal purple 75-140 synthetic and changed both tranny filters and did 2.5 qts royal purple and 4 quarts ATF+4. I also added a drain plug to the tranny pan.
this thing drives so well, and more parts to come.