- Location
- Virginia City, NV
Figured im starting another chassis build even though it will have the same components underneath. Its going to be a fresh start for me to do all the reinforcements i wanted to do before i started wheeling the rig.
So the plan for this rig is to do frame stiffeners front to rear. So far i have tnt mid, dirtbound rear, and some fronts i found on ebay. I will also be doing boatsides with 2x6 sliders welded in. Then i will be doing an xo fab hybrid cage and rear quarter armor. Ill be building my own front bumper and modifying my current crock4x4 rear bumper. Gonna be doing a rear cut and fold and clearancing for the 37s with a bit more finesse and planning. So. Fist off a few pics
Here is my starting point. 97 two door 2wd auto with a blown head gasket and 150k miles. It had a tree fall on the cowl area so the a pillars need a little massaging. That will be done before the cage goes in.
So today i dove in and found the problem with the head gasket. Found the culprit for sure. I did a mps felpro premium gasket when i threw it back together. New head-bolts and gaskets all around. Not sure if ill keep this motor in here but i want to get it running first and see how it runs.
Got it all sealed back up tonight. Gonna do the water pump and water neck in. The morning and fire it up tomorrow. Ill keep updating. If all goes well ill be welding in the stiffeners this week.
So the plan for this rig is to do frame stiffeners front to rear. So far i have tnt mid, dirtbound rear, and some fronts i found on ebay. I will also be doing boatsides with 2x6 sliders welded in. Then i will be doing an xo fab hybrid cage and rear quarter armor. Ill be building my own front bumper and modifying my current crock4x4 rear bumper. Gonna be doing a rear cut and fold and clearancing for the 37s with a bit more finesse and planning. So. Fist off a few pics


Here is my starting point. 97 two door 2wd auto with a blown head gasket and 150k miles. It had a tree fall on the cowl area so the a pillars need a little massaging. That will be done before the cage goes in.
So today i dove in and found the problem with the head gasket. Found the culprit for sure. I did a mps felpro premium gasket when i threw it back together. New head-bolts and gaskets all around. Not sure if ill keep this motor in here but i want to get it running first and see how it runs.



Got it all sealed back up tonight. Gonna do the water pump and water neck in. The morning and fire it up tomorrow. Ill keep updating. If all goes well ill be welding in the stiffeners this week.