Re: What was done to YOUR rig today MECHANICALY????
Rumor has it that it has gotten cold in these here parts lately!
Changed the plugs, rotor, cap and air filter in my 87. Found a funky electrical connection on one injector, this week, took it for a test drive today. One interesting note, it was driven the last 18 months or so with two different single platinum tip brands of spark plugs. 2 were Autolite and 4 were Bosch. The Bosch still looked brand new-clean, the Autolites had some carbon fouling, front two cylinders. The Cap and rotor were on their last legs, wires were still good, not very old yet. Idle has dropped from 750 to 550 for as yet unknown reasons.
89 is acting like it is ready for another Dex III transfusion, and the leak must have stopped, as it is still too full (hot) since I last brought the level back up, 2500 miles or so ago. Reverse still does not like the cold weather. It got a new tire last week and replaced the fuel pressure regulator about week ago which solved some rough idle problems...it was leaking fuel into the vacuum line!