87xjco
NAXJA Forum User
- Location
- Denver, CO
John (IoN6 on CO4X4) has a 1979 CJ5 Golden Eagle that is going thru a major overhaul.
He brought me a HP44 with Yukon 4.10 gears and an ARB locker for install.
Unfortunately John didn't bring me the old pinion gear and carrier. This makes a few things more difficult to set up.
Since I did not have the old pinion and was not able to determine what oil slingers were in place originally and I was not able to measure for shim thickness. This meant I was going to have to install from memory what slingers I believe the front HP44 came with and I was probably going to have to try several different shim stacks, before I obtained a good pinion depth.
Unlike the typical rear D44 pinion gear shown below, every front D44 I have done so far has a large slinger that is installed between the inner bearng and the back side of the gears, they also have a smaller stepped slinger that installs between the inner bearing race, and the axle housing.
So I pressed his new inner pinion bearing on with the large slinger in place, and added .045" of shims between the bearing and the stepped slinger, I knew I was probably going to have to make several changes in shim thickness, so I used a set up inner bearing race that has the outside surface ground off and will slide into the housing by hand.
Here's the set up, 3 - .010" shims and 1- .015" shim and the stepped slinger and set up race.
I installed the pinion into the housing leaving out the shims that are used for setting pinion bearing pre-load (I will set that after the pinion depth is dialed in), I tightened down the pinion nut until there is a little bit of force required to turn the pinion by hand.
In the mean time John installed the new ring gear onto the ARB and torqued the bolts in a star pattern to the proper torque spec.
I then installed the carrier into the housing, I was not concerned about having proper backlash at this time, as long as I had some backlash, I could run the pattern and work on pinion depth. Pinion depth always has to be set properly first before set up of pinion bearing pre-load or backlash.
Here's the first pattern and not surprisingly it needs alot of adjustment, it's hard to see in this photo but the pattern is showing contact on only a portion of the inner edge, indicating the pinion is too deep.
So it came back apart and I removed .015" of shims, re-installed and ran the pattern again. Now the pattern indicates the pinion is a little to shallow.
The coast side looks pretty good
So it came apart again and I removed a .010" shim and installed this .006" shim,
Then I reassembled everything and ran the pattern again.
Third time is the charm. Hard to see again but the lines indicate the edges of the pattern.
And the coast side still looks good
Now its time to take everything apart, remove the set up race and install the new race, then I installed .040" worth of shims between the outer pinion bearing and the shoulder of the pinion gear, tightened down the pinion nut until I started to feel drag on the pinion, I found I was getting too much rotational force before the pinion nut was all the way tight.
This meant I needed to add some more pre-load shims, I add .006" of shims, re-tightened and that worked good.
My close up photography really sucked last night, but the blue arrow indicates the max. torque obtained when rotating the pinion and it is slightly more that 17in lbs. Perfect.
So now its time to install the carrier and set back lash. I started with .060" shims on the teeth side of the carrier, and .025" on the bolt side. The carrier was snug going in and required tapping it most of the way in with the dead blow hammer and using the caps to pull it in the rest of the way. That's just how I want it, to insure carrier bearing pre-load is good.
My first dial indicator reading showed about .015" and that's too much.
So I changed the teeth side to .055" and added .005" to the bolt side of the carrier.
Then I obtained the below readings. Good .0065" backlash
So you might think I was all done, so did I.
But for good measure I ran the pattern again and found it was way off. The only thing that changed since I last checked it, was removal of the set up race and installation of the new race. Well I took it all back apart, measured the two races and they were the same thickness.
Scratching my bald head trying to figure out what happened, I don't know but I know I am gonna have to change shims again until it is right. I ended up taking .010" out of the inner bearing shim pack, doing the same to the outer bearing pre-load pack Cussed a few times (o/k alot) and then a couple more thousands shim adjustments for correct pinion bearing preload.
Then I re-installed the carrier, Cussed a few more times (o/k alot), made a few more shim adjustments to bring the backlash back in spec. And then we ran the ARB line thru the case.
Thinking about it last night, I think the problem with the set up race is that because it doesn't fit tightly into the case, it isn't able to fully compress the shim pack, and this gave me a false reading. But the problem with not using a set up race is that everytime you have to use a punch to knock out the new race, you destroy the slinger that goes between the race and the housing. Luckily I had a couple of extra ones.

He brought me a HP44 with Yukon 4.10 gears and an ARB locker for install.
Unfortunately John didn't bring me the old pinion gear and carrier. This makes a few things more difficult to set up.
Since I did not have the old pinion and was not able to determine what oil slingers were in place originally and I was not able to measure for shim thickness. This meant I was going to have to install from memory what slingers I believe the front HP44 came with and I was probably going to have to try several different shim stacks, before I obtained a good pinion depth.
Unlike the typical rear D44 pinion gear shown below, every front D44 I have done so far has a large slinger that is installed between the inner bearng and the back side of the gears, they also have a smaller stepped slinger that installs between the inner bearing race, and the axle housing.

So I pressed his new inner pinion bearing on with the large slinger in place, and added .045" of shims between the bearing and the stepped slinger, I knew I was probably going to have to make several changes in shim thickness, so I used a set up inner bearing race that has the outside surface ground off and will slide into the housing by hand.
Here's the set up, 3 - .010" shims and 1- .015" shim and the stepped slinger and set up race.

I installed the pinion into the housing leaving out the shims that are used for setting pinion bearing pre-load (I will set that after the pinion depth is dialed in), I tightened down the pinion nut until there is a little bit of force required to turn the pinion by hand.
In the mean time John installed the new ring gear onto the ARB and torqued the bolts in a star pattern to the proper torque spec.
I then installed the carrier into the housing, I was not concerned about having proper backlash at this time, as long as I had some backlash, I could run the pattern and work on pinion depth. Pinion depth always has to be set properly first before set up of pinion bearing pre-load or backlash.
Here's the first pattern and not surprisingly it needs alot of adjustment, it's hard to see in this photo but the pattern is showing contact on only a portion of the inner edge, indicating the pinion is too deep.

So it came back apart and I removed .015" of shims, re-installed and ran the pattern again. Now the pattern indicates the pinion is a little to shallow.

The coast side looks pretty good

So it came apart again and I removed a .010" shim and installed this .006" shim,

Then I reassembled everything and ran the pattern again.
Third time is the charm. Hard to see again but the lines indicate the edges of the pattern.

And the coast side still looks good

Now its time to take everything apart, remove the set up race and install the new race, then I installed .040" worth of shims between the outer pinion bearing and the shoulder of the pinion gear, tightened down the pinion nut until I started to feel drag on the pinion, I found I was getting too much rotational force before the pinion nut was all the way tight.
This meant I needed to add some more pre-load shims, I add .006" of shims, re-tightened and that worked good.
My close up photography really sucked last night, but the blue arrow indicates the max. torque obtained when rotating the pinion and it is slightly more that 17in lbs. Perfect.

So now its time to install the carrier and set back lash. I started with .060" shims on the teeth side of the carrier, and .025" on the bolt side. The carrier was snug going in and required tapping it most of the way in with the dead blow hammer and using the caps to pull it in the rest of the way. That's just how I want it, to insure carrier bearing pre-load is good.
My first dial indicator reading showed about .015" and that's too much.
So I changed the teeth side to .055" and added .005" to the bolt side of the carrier.
Then I obtained the below readings. Good .0065" backlash

So you might think I was all done, so did I.
But for good measure I ran the pattern again and found it was way off. The only thing that changed since I last checked it, was removal of the set up race and installation of the new race. Well I took it all back apart, measured the two races and they were the same thickness.
Scratching my bald head trying to figure out what happened, I don't know but I know I am gonna have to change shims again until it is right. I ended up taking .010" out of the inner bearing shim pack, doing the same to the outer bearing pre-load pack Cussed a few times (o/k alot) and then a couple more thousands shim adjustments for correct pinion bearing preload.
Then I re-installed the carrier, Cussed a few more times (o/k alot), made a few more shim adjustments to bring the backlash back in spec. And then we ran the ARB line thru the case.

Thinking about it last night, I think the problem with the set up race is that because it doesn't fit tightly into the case, it isn't able to fully compress the shim pack, and this gave me a false reading. But the problem with not using a set up race is that everytime you have to use a punch to knock out the new race, you destroy the slinger that goes between the race and the housing. Luckily I had a couple of extra ones.