Follow along with the video below to see how to install our site as a web app on your home screen.
Note: This feature may not be available in some browsers.
Welcome to the new NAXJA Forum!
If your password does not work, please use "Forgot your password?" link on the log-in page.
Please feel free to reach out to [email protected] if we can provide any assistance.
well i trusted somebody to cut my tcase shaft down to make a hack and tap and he's had it for 2 months now he won't return my shaft or answer calls so i'm in need of another shaft.....lemme know what you have. would even take a full case if i had to and the price was right
turns out the computer was putting voltage out on both sides of the cam sensor whether it was running or not. not sure if that was the whole problem since i cut out the stock setup and installed a megasquirt 3 but it kinda makes sense
turns out my no start is a no fuel issue. think i've got a clogged strainer or filter cause i can hear the pump plain as day....i'll mess with it tomorrow when i'm feeling better
yup fixed those already. i followed all the grounding mods in cruiser's link and verified ohm's in multiple places before i sealed everything up. highest resistance was .2 ohms when i was done. lowest was .05
oh and i'm starting to think ecomike is right about it being the tps but i don't know how to fix it. it's set right according to cruisers page but now it idles at 300-400 and tries to die everytime i take my foot off the peddle
yes it does. i plugged the cps into it by mistake and the jeep wouldn't run
cruiser my distributor lines up exactly like the 1 in the pic on your link....exactly
the cat's brand new but i do have an exhaust restriction. running 2.25" down pipe to 2.5" cat and muffler to 2.25" tailpipe. soon as i get more money i'll get the tailpipe replaced and until i can afford a new header there's no point in changing the downpipe
stroker stats
kb944 pistons .020...
my rotor is pointed exactly like that 1
driveability is fine except it still won't rev. shifts fine pulls like a stroker should. had it up to 70 with no issues about an hour ago. i'm starting to think the ecm just can't handle the new motor
installed the old distributor and went 1 tooth...